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| Build a Hybrid Tube Amplifier to drive Electrostatics (1976) |
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AFTER COMPLETING MY electrostatic speakers and KEF/transmission line woofers, it became time to consider an amplifier for the ESLs. I had been using a Williamson "twin 20" driving some old output transformers (in reverse) with excellent results. A direct coupled amplifier offered a small, but perceptible improvement as demonstrated by direct sonic comparison with David Hermeyer's original high voltage, direct coupled electrostatic amplifier (see Issue #4, 1972 series, p.9). As this project was designed to offer the finest sound quality, I felt any improvement possible should be inclined. When I decided to use a direct coupled amplifier I had to face the problem of building one, of course. Unfortunately, Dave's original design was unacceptable to me. My reasons? It is physically just too huge, it wastes too much electricity, and it puts out enormous amounts of heat. My wife is not exactly keen on Dave's amp either, for all the above reasons and because she thinks it is ugly.
1. Use 8068 beam pentode output tubes, rated at 3.5kV at 35 watts. These are normally used as high voltage series regulators and cost about $5.30 each (the original 813 costs about $35.) The 8068 uses a standard 8 pin octal socket which cost less than 50¢ each. 2. Each filament requires 6.0 to 6.3V AC @ 0.9 amps. Little 6.3V AC transformers are easily obtainable, but I chose to use the standard Triad (#F34A) transformer which has four separate secondaries rated at 6.3V AC @ 1.75 amps each. The transformer costs about $12 and is about the size of a cube with 3" sides and comes with end bells standard. I have seen these surplus 3. The 8068 is 4 5/8" tall, 4" seated, 1 9/16" in diameter, and has an indirectly heated cathode. Connect as per schematic. The 2700, lW cathode resistor may be carbon type. 4. Grid 2 (screen) should be +200 V DC with a 100ma supply for four tubes. As this 100ma is not being drawn constantly I opted to use a 25ma continuous rated supply and have had no trouble with it overheating. 5. Instead of two 250K series resistors rated at 5 watts (metal oxide film types) as the feedback loop attenuator, use ten 50K (47K is fine) resistors in series rated at 1 watt. These should be identical metal film types. The reason? Reduced distortion. As Dave explains it to me, resistors have a voltage coefficient (similar to a temperature coefficient) which makes them non-linear if they have a high voltage drop across them. Carbon is the worst in this respect and metal oxide film is the best (but not perfect). Splitting the voltage drop across many resistors minimizes this effect. In my amp, each resistor drops a maximum of 220 volts. As the feedback to the input must accurately reflect the output signal, great linearity is obviously required for maximum performance and lowest distortion. This is one reason why I believe the performance of my amp may be better than the original design. 6. Metal oxide film resistors in locations with asterisks on the schematic will also improve the performance.
Fig. 2
8. The original +100 volt supply for the circuit board drive components is now reduced to +80 volts. The same semiconductors are still used, so the drivers do not get so hot (although the small heat sinks are still necessary). I had a great deal of difficulty finding a small transformer to use in this supply. Only 100ma is required (8 watts) and as space was critical I wanted a transformer that was just big enough that would be in the range of 60 to l20V AC. I finally gave up, took a small 6.3V AC filament transformer apart and rewound it. I had never wound a transformer before, but I followed the directions in the latest edition of The The other transformer seen there is for the 12V DC power supplies. All the other transformers I used were surplus military hermetically sealed units. I love quality, and besides, they look so nice! I was lucky enough to find a 2kV sealed unit @ 20ma for the bias supply, but if I hadn't I would have wound a tiny, high voltage transformer exactly as I had done the 63 volt unit, and I would have used a voltage doubler or tripler to get the necessary voltage (2kV of bias is plenty). To avoid the large 5 watt pot used to regulate the voltage of the bias supply, I used a standard pot in series with a fixed wirewound, 5 watt resistor. This required one resistor change to get a suitable value, but it works fine. Connect it as in Fig.2. By using a completely series connection (as opposed to paralleling one resistor across the line as shown in Dave's original article) there is even less current drawn through the t watt pot and it does not even get warm. 9. The big B+ power supply in Dave's original amp seemed too complex and unreliable because of all the parts required and because of all those perishable electrolytic capacitors, making it too big. So I turned to the trusty Radio Amateur's Handbook and designed a different power supply. Right off I' noticed that with all those 500vF capacitors in series, Dave achieved a total of only 62.5 vF capacity! Not really very good filtering, although obviously adequate. I was determined to do better than that. The string of capacitors would have to go, and more reliable ones rated at the full power supply voltage would have to be used. I ended up using 7vF oil capacitors rated at 2.6kV. I chose a reactor filter so would not need high capacity but would still achieve superb filtering (Fig.3). Lastly, I wanted to eliminate those strings of diodes for the high voltage rectifiers. I was able to locate surplus 10kV @ 1 amp (conservative again!) diodes for $14 per four. These can be obtained from Electro-Science Mart or B & F Surplus. My oil capacitors were new and cost almost $10 each from Electro-Sales. These oil capacitors are quite small for 2.6kV units @ 7vF but have the disadvantage that their contacts are metal straps with one connected to the case. Therefore they must be insulated from the chassis. I took four of them and soldered them to each other (the fifth is on the other side of the reactor). I drilled a piece of 1;" Plexiglas to accept the metal straps from the center of the capacitors. Then I punched chassis holes considerably larger than those in the Plexiglas so the Plexiglas formed an insulating ring when the capacitors were mounted with their tabs extending through the chassis. I glued the capacitors to the Plexiglas with 24-hour epoxy and attached this strong, rigid assembly to the chassis with bolts. Capacitor connections were made with high voltage test prod wire. I placed an Amperite 45 second delay relay in the AC line to the B+ transformers. This delays the B+ automatically until the 8068' s heaters get hot. This also allows easy testing since removing the relay tube from its octal socket makes the B+ inoperative. I quickly discovered that the B+ load ate delay relays in the ESL amp. The solution was to add a relay that was operated by the delay relay (see Fig.3B). I set it up so that three of the four contacts (rated at 3 amps) are paralleled for handling the B+ with the fourth contact used to disconnect the delay relay power so that it resets and the full delay is obtained should the amp be rapidly switched on and off (kids). I used a Potter and Brumfield 4pdt relay with a l20V AC coil. The 5K resistor keeps the delay relay contacts from delivering significant current to the Issue 1/1976 15 B+, but allows enough to keep the secondary relay pulled in after the delay relay contacts open. The system is now an "all or none" system: it either turns on or it doesn't. Comments Another problem with associated equipment is oscillation. Exactly why the amplifier should cause other equipment to oscillate is unclear to me. In any case, the amplifier is completely stable when driven by some equipment, and very unstable when driven by other equipment. The instability ranged from "motor boating" or high frequency squeal to just crackling or chirping on loud, high frequency transients. In the case of the Old Colony crossover I found that a 3dB corner of 68 kHz worked very well. In addition, a 600n resistor should be added to the output so that the output impedance is stabilized and the amp output can be stabilized for essentially zero offset. I also added some equalization components (detailed in Issue #4, 1975 series, pp.24 ff.) boosting low frequencies to compensate for the phase cancellation at low frequencies and beaming effects of the speaker.I am currently using 12dB/octave crossovers and find that rolling off the ESLs at 240Hz and rolling off the KEF woofers at 120Hz is about right. Using identical crossover points does not work well in this system because the ESLs' fundamental resonance is bringing up their level in the crossover region, which when combined with the woofer output gives an undesirable and annoying peak in the mid bass. I would guess that the effective subjective crossover point is around 150Hz. I have more experimenting to do in this area. It will be interesting to see what faster ICs and steeper slopes do to the sound, for example. The amp was carefully designed to stay cool, and I'm pleased to say I was successful in this regard. The plate resistors run at extremely high temperatures, so I kept them completely away from everything else and out in the open so they wouldn't conduct heat to the chassis. I didn't want to use a fan, so I mounted the tubes on the extreme edge of the chassis and punched 1" holes completely through the chassis for free air flow. The tubes do not seem to get excessively hot and can even be touched for a second or two without burning you. The power transformers in the B+ supply gradually heat up the whole amp, hut it never gets more than comfortably warm except on the transformers themselves. I also did not use a perforated cover on the amp because the tubes and plate resistors would greatly heat this, making the whole amp very hot after a time. I decided instead to use sealed components and have all high voltage wiring under the chassis. As the components are rather heavy for an aluminum chassis which looks like Swiss cheese after cutting the mounting holes, I used a h" aluminum bottom plate which is secured every 3 inches with a screw as you can see in the photo below. SUPPLIERS
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